Spent a half day with Clay adjusting timing and carbs. Got the car running better but it still hesitated at partial throttle. Greg decided since he intended to convert to Pertronix electronic ignition anyway, let's proceed with this plus a new ignition coil since the root cause seemed to be ignition related.
Parts came in, but now car won't start even before we install the new parts. Determined no fuel, further discovered the fuel gauge sending unit was installed upside down so even though it said full it was really empty. Matter of fact, it ran completely out of fuel about one minute after arriving back at the shop. Hence much confusion - why doesn't it run? No fuel. But the gauge says full. Put gas in tank, fired right up. Go figure.
Then got new ignition parts installed, finally this car runs awesome! Hesitation all gone. Meantime installed new steering rack boot on one side plus door interior pulls.
The one final major concern is the squealing noise from the clutch. Clutch works fine and most times does not squeal, just squeals occasionally when hot and engaging first gear or reverse. Put the car on the lift, double checked slave cylinder bolts to make sure they weren't too long (touching clutch diaphragm), decided to pull back rubber boot on throwout bearing lever and - found a mouse nest in the bell housing! Removed about a handful of fluffy material. It appears the mice got in there through the opening for the starter motor. Since removing this much material it appears the squealing is getting less severe. Still confused over how this material can cause an occasional squeal. All clutch parts or made of metal and should shred mouse nests and mouse carcasses to powder. Greg is taking the car home and will just drive it and then in another week or so we'll put the car on the lift, pull the lever boot back, and see if we can get more mouse nest material out.
Meantime, Saturday 9/22 was the annual British Car Show. This car was there, here's some pictures from when Ray cleaned up the car the day before:
Saturday, September 22, 2018
Tuesday, September 4, 2018
Good tip, Clay!
My friend Clay suggested that I confirm that the vacuum and mechanical advance functions were working on the distributor. Turned out to be a good tip. Here's a section of the vacuum line that had fallen behind the motor and gotten burned up:
It was sealed, so at least it was not a vacuum leak. But the distributor was definitely not advancing it's timing with vacuum increases! Guess there's a reason the factory made these lines out of metal.
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I patched it back together and checked it's operation with a vacuum pump and found that it still did not work because the small spring that connects the vacuum diaphragm to the distributor plate inside the distributor was disconnected. Got that repaired, went out and drove car, and it's much better. Still want to confirm dwell and timing adjustments and then fine tune the carb settings, but we're getting much closer now.
Monday, September 3, 2018
Check air, then spark, then fuel
Air, spark fuel - that's the sequence that I learned from my MG technical sessions I have attended. So I started with air - checked all valve clearances (no major problems but had to adjust 6 of the 8 to get consistent 0.015" gap). Then checked compression - 150, 160, 155, 150 from front to back. This is excellent.
My dwell meter pooped out on me, so could not really confirm points gap. And could not then confirm timing. All indications are spark is OK though, so I violated the tech seminar and went on to fuel. : )
Pistons move easily, but jet position was way too low on the back carb. Corrected that, then confirmed the fuel level in the jets is about right for both carbs, ie float levels set right. Front carb did seem kind of dry, but it's float was set for deeper fuel level than rear. I ran car in garage, idles fine and revs up fine, saw good atomized fuel flow into throat of carb when revving engine. But took it out and it still bogs down and hesitates under load. Decided to take up my friend Clay's offer to bring car to him and connect it to his diagnostic equipment,made appointment for a week away unfortunately due to our schedules.
Had a little more time to I tackled the logo on the trunk lid. There are 15 little holes that need to be in the trunk to install the four pieces of the logo. These were all filled in with body filler, so they were completely invisible on the outside. But you could see them from the back side. So with some trepidation I drilled out all 15 holes very carefully. I also bought some plastic screw anchors which do a decent job of retaining the pieces in place, should be using a speed clip. Here's a sample of the plastic piece:
Here's the backside after installation:
Those little pieces worked pretty well. Here's now the pretty side:
Those white stripes are the lights of my garage. Turned out real well!
My dwell meter pooped out on me, so could not really confirm points gap. And could not then confirm timing. All indications are spark is OK though, so I violated the tech seminar and went on to fuel. : )
Pistons move easily, but jet position was way too low on the back carb. Corrected that, then confirmed the fuel level in the jets is about right for both carbs, ie float levels set right. Front carb did seem kind of dry, but it's float was set for deeper fuel level than rear. I ran car in garage, idles fine and revs up fine, saw good atomized fuel flow into throat of carb when revving engine. But took it out and it still bogs down and hesitates under load. Decided to take up my friend Clay's offer to bring car to him and connect it to his diagnostic equipment,made appointment for a week away unfortunately due to our schedules.
Had a little more time to I tackled the logo on the trunk lid. There are 15 little holes that need to be in the trunk to install the four pieces of the logo. These were all filled in with body filler, so they were completely invisible on the outside. But you could see them from the back side. So with some trepidation I drilled out all 15 holes very carefully. I also bought some plastic screw anchors which do a decent job of retaining the pieces in place, should be using a speed clip. Here's a sample of the plastic piece:
Here's the backside after installation:
Those little pieces worked pretty well. Here's now the pretty side:
Those white stripes are the lights of my garage. Turned out real well!
Sunday, September 2, 2018
Top Installed, First Car Wash
Decided a really hot day like today would be a good time to install the top, it seemed like it would be a tight fit and it was. But I got it on, and will leave it one for a while to let it stretch into the position for this car. This was a very good used top we bought earlier.
Then I decided I couldn't stand the myriad greasy fingerprints on the car, so I washed it off. Had to clean a little white stuff off the top too, not sure what it was. Turned out real good, I think:
Now I need to get this thing to run right......
Then I decided I couldn't stand the myriad greasy fingerprints on the car, so I washed it off. Had to clean a little white stuff off the top too, not sure what it was. Turned out real good, I think:
Now I need to get this thing to run right......
Friday, August 31, 2018
A good half day's work
Started out checking into the brake issue. I could see nothing wrong or interfering with the brake pads. But I did notice that the new pads hit on parts of the rotor that the old pads did not. We did not turn the rotors, so this leaves these rusty areas for the pads to hit. I tried to capture it in this picture:
I cleaned up the rusty portions on the outside of the rotors on both sides with sandpaper. Can't get to inside due to dust guard. Took the car out and drove it. First few applications of the brakes were just fine. But later they starting squeaking again, not quite as bad as yesterday. So I suspect just driving the car and wearing down these rusty portions of the rotor will resolve this issue.
Installed some other parts. New shifter rubber and leather boot:
The leather works out kinds funky with the short shifter. I installed the snaps to hold the footwell carpeting in place too.
I cleaned up the chrome rings on the gauges on the dash, looks good:
I also took apart the plastic shroud over the column to see why the turn signals don't cancel. It appears they should cancel, but that portion of the switch assembly no longer functions. A new switch costs about $30, so it's not worth trying to repair the old one. So either Greg lives with the non cancelling turn signals or spends another $30! This decision can be delayed.
Installed new spark plugs and drove car. It still has a large hesitation when accelerating. Need to put some more thought into how to resolve this one.
I cleaned up the rusty portions on the outside of the rotors on both sides with sandpaper. Can't get to inside due to dust guard. Took the car out and drove it. First few applications of the brakes were just fine. But later they starting squeaking again, not quite as bad as yesterday. So I suspect just driving the car and wearing down these rusty portions of the rotor will resolve this issue.
Installed some other parts. New shifter rubber and leather boot:
The leather works out kinds funky with the short shifter. I installed the snaps to hold the footwell carpeting in place too.
I cleaned up the chrome rings on the gauges on the dash, looks good:
I also took apart the plastic shroud over the column to see why the turn signals don't cancel. It appears they should cancel, but that portion of the switch assembly no longer functions. A new switch costs about $30, so it's not worth trying to repair the old one. So either Greg lives with the non cancelling turn signals or spends another $30! This decision can be delayed.
Installed new spark plugs and drove car. It still has a large hesitation when accelerating. Need to put some more thought into how to resolve this one.
Thursday, August 30, 2018
Driving the Car!
Ray and Greg were able to install the passenger seat and carpet while Vince was traveling earlier this month:
Today Vince installed the new Grose float valves plus he created copper tubes as float chamber overflow pipes. We had an issue with the old float valves leaking, which then dripped on the exhaust manifold, not good. No leaks with these new style float valves, but even if they do leak it will now dribble out the bottom of the car safely!
Vince then, with some trepidation, took off to drive the car from Boonville to his home in Evansville! First significant drive of the car in we believe about 40 years, went 12 miles on a very hot day. I made it, although the car did hesitate a little at part throttle. It was then I remembered we had not replenished the oil in the carb dampers. Oops! After getting home I filled them up and it got MUCH better, still not perfect yet though. Probably need some new spark plugs too.
There's a very loud squeal coming from the front brakes when applied hard, sounds like metal on metal, hopefully this is something obvious and easy to fix.
Despite the heat the car ran about 185 and had great oil pressure. Tranny and clutch all worked fine, wheel balance is pretty darn good, got it up to 65 with no vibration. Quite a few little items to still work on, but this is a major step!
Here's the car in it's new temporary home:
Today Vince installed the new Grose float valves plus he created copper tubes as float chamber overflow pipes. We had an issue with the old float valves leaking, which then dripped on the exhaust manifold, not good. No leaks with these new style float valves, but even if they do leak it will now dribble out the bottom of the car safely!
Vince then, with some trepidation, took off to drive the car from Boonville to his home in Evansville! First significant drive of the car in we believe about 40 years, went 12 miles on a very hot day. I made it, although the car did hesitate a little at part throttle. It was then I remembered we had not replenished the oil in the carb dampers. Oops! After getting home I filled them up and it got MUCH better, still not perfect yet though. Probably need some new spark plugs too.
There's a very loud squeal coming from the front brakes when applied hard, sounds like metal on metal, hopefully this is something obvious and easy to fix.
Despite the heat the car ran about 185 and had great oil pressure. Tranny and clutch all worked fine, wheel balance is pretty darn good, got it up to 65 with no vibration. Quite a few little items to still work on, but this is a major step!
Here's the car in it's new temporary home:
Thursday, July 19, 2018
Seats, Steering Wheel, and Front End/Wheel Balance
Greg finished up the steering wheel with it's leather cover, turned out very nice:
Also the door panels are installed, carpet on inner sills, and rubber trim installed around door opening:
Seats are done and ready to be installed, a friend ended up donating some better used foam cushions which worked out just fine:
Interestingly, the red piping didn't line up real well from seat back to seat bottom until we swapped the seat backs between the two seats - wonder if they had been switched before? They line up much better this way, passenger seat on left is well aligned while driver's seat on right is about 3/8 inch off. Very comparable to our other MGB's.
When we had the tires mounted we were told the tire shop could no longer balance wire wheels, their newer wheel balancer might mess up the splines. They claimed this is a problem with all newer wheel balancers. We had been given an old manual wheel balancer but knew we were missing some pieces of it - called the donor and got the missing pieces. This thing works real well, here's a picture of the old Snapon model WBK-2:
It even came with a good selection of weights. So today we got all four wheels balanced plus adjusted the front end to 1/8 inch toein. We're getting very close to getting this thing on the road! Unfortunately we need seats installed to drive it, and it's much easier to put in carpet and side panels in wheel wells without the seats in place. Patience, patience.
Also the door panels are installed, carpet on inner sills, and rubber trim installed around door opening:
Seats are done and ready to be installed, a friend ended up donating some better used foam cushions which worked out just fine:
Interestingly, the red piping didn't line up real well from seat back to seat bottom until we swapped the seat backs between the two seats - wonder if they had been switched before? They line up much better this way, passenger seat on left is well aligned while driver's seat on right is about 3/8 inch off. Very comparable to our other MGB's.
When we had the tires mounted we were told the tire shop could no longer balance wire wheels, their newer wheel balancer might mess up the splines. They claimed this is a problem with all newer wheel balancers. We had been given an old manual wheel balancer but knew we were missing some pieces of it - called the donor and got the missing pieces. This thing works real well, here's a picture of the old Snapon model WBK-2:
It even came with a good selection of weights. So today we got all four wheels balanced plus adjusted the front end to 1/8 inch toein. We're getting very close to getting this thing on the road! Unfortunately we need seats installed to drive it, and it's much easier to put in carpet and side panels in wheel wells without the seats in place. Patience, patience.
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